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Alias Born 04/12/2021

Re: None

Wednesday, 02/15/2023 6:41:49 AM

Wednesday, February 15, 2023 6:41:49 AM

Post# of 5636
Tweets were steady in 2022, but then abruptly stopped in November; was the company sold?

“Mdmpermian
@mdmpermian
·
Feb 14, 2022
Field Update: Brown #1 well has had 1207 bbls swabbed into frac tank. Had pump delivered and running rods. We can pump over 200 bbls per day which is close to what we have been getting from swabbing. Pump will be set 70 feet above top perforation. $MDMP #MDMP
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mdmpermian
@mdmpermian
·
Feb 11, 2022
Field Update: Brown #1, we swabbed 120 bbls by lunch. Good news - we have started to get oil odor in samples. Will swab more today and shut in for weekend. $MDMP #MDMP
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mdmpermian
@mdmpermian
·
Feb 11, 2022
Field Update: Brown #1 so far recovered 1010 bbls of frac fluid load end of Thurs. opened this am at 800 ft from surface again. Starting swabbing. More to come later today. $MDMP #MDMP
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mdmpermian
@mdmpermian
·
Feb 10, 2022
Field Update: Brown #1 well had 18 swabs so far today. Recovered 111 bbls of gassy frac fluid. Fluid level in well is holding at 1400 ft from surface. Top perforation is at 6314 ft. Continuing to swab and monitor.
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mdmpermian
@mdmpermian
·
Feb 10, 2022
Field Update: Brown #1, well flowing through casing overnite. Shut in casing and pulled 5 swabs in first hour, got 25 bbls. Fluid level holding at 800 ft from surface and gassy. 790 barrels recovered so far from 3140 bbls pumped on frac. Continuing to swab well. #MDMP $MDMP
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mdmpermian
@mdmpermian
·
Feb 9, 2022
Field Update: Brown #1 has tubing to the perfs and rig is swabbing 3 to 4 times per hour. Over 700 barrels total recovery so far! Transports coming to empty tanks. #MDMP $MDMP”

my posts are always theory and not financial advice