InvestorsHub Logo
Followers 5
Posts 434
Boards Moderated 0
Alias Born 09/30/2020

Re: None

Friday, 02/10/2023 10:10:35 AM

Friday, February 10, 2023 10:10:35 AM

Post# of 1866
WEEKLY DRILLING REPORT FEBRUARY 9, 2023
WELL: Guluc-2

Spudded December 10, 2022. Days since spud: 61
Progress: 0
Measured Depth: 3910 metres
Week Summary:

RIH with casing scraper to prepare borehole for completion string, took 2 days
RIH with cement bond logging, took 2 days
RIH with 4 ½ “ tubing completion string, over 2 days, but wait on weather (WOW) as 40 knot winds and high seas
Set production packer at 3410 metres, measured depth, pressure test, and did inflow test, both good and pass
Further Activities:
Perforate the lower gas interval and test well
Turn over to Production Operating Partner
Side RIG over a few feet to continue with the West Akcakoca-1 well, which already has 1008 metres of surface hole drilled.

The well Guluc 2 is the longest well at MD of 3910 metres and has a very long, almost horizontal (only a slight incline) section. To move the Cement Bond logging tool and the completion string, the UltraTrac all-terrain well tractors are used to convey the equipment down hole in the well. Using them is more efficient compared to pushing with a full drill pipe. Almost all of them in the world are contracted out, but we planned for this and have 5 for our drilling program. Due to the extended length of the well, it takes a little more time to go from the surface to total depth. However, we will be perforating shortly and putting Guluc 2 on production.
Volume:
Day Range:
Bid:
Ask:
Last Trade Time:
Total Trades:
  • 1D
  • 1M
  • 3M
  • 6M
  • 1Y
  • 5Y
Recent TRLEF News