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Re: FISH1031 post# 231

Saturday, 02/14/2009 11:13:28 AM

Saturday, February 14, 2009 11:13:28 AM

Post# of 244
Are we happy now !!! NO, this from there Dec 18 PR

The John Bowen #2 Well Deep Gas Test: Montello has been monitoring the deep gas zone which has flowed mud filtrate and drilling fluid into the wellbore with an associated gas blow. In an attempt to facilitate hydrocarbon inflow into the wellbore, Montello has just completed a Nitrogen gas fracturing operation on the deep gas zone. Subsequent to the Nitrogen frac, inert gas was recorded at surface. The well will be shut-in for a period of three to four weeks to allow a pressure build-up prior to re-opening the wellbore. Montello believes that the well bore sustained skin damage at the deep gas interval and will be investigating remedial options.

This is where they went side ways in the drilling of this well to save it , around 7800 ft and then in to the Rome formation. The skin damage may of seal off the gas at this level and this well.

I m not sell the first share here, WHY because there six other zone that show good pressures higher up the pipe. As you all know I got the logs on this well and only the ones that are not inform are selling or not thinking to clearly at this point.

When I talk too Bill C back in the fall they had 9 formation behind pipe to get in to production, this is only one of them 9.

Yes this is a let down and thing need to change with this company as who they go into deals with, I think that waiting a hole year to finniest this well did not help at all.

FISH